mars 202435 Lessons Learned Instruction Manual
- July 13, 2024
- MARS
Table of Contents
- mars 202435 Lessons Learned
- Product Information
- Product Usage Instructions
- MARS 202435
- MARS 202436
- MARS 202437
- MARS 202438
- MARS 202439
- MARS 202440
- Lessons learned
- Frequently Asked Questions
- Q: How can I ensure safe bunkering operations?
- Q: What should I do in case of a chemical exposure incident?
- References
- Read User Manual Online (PDF format)
- Download This Manual (PDF format)
mars 202435 Lessons Learned
Product Information
Specifications
- Product Name: MARS Report No 381
- Issue Date: July 2024
- Product Code: MARS 202435, MARS 202436, MARS 202437
Product Usage Instructions
Collision in daylight and good visibility (MARS 202435)
The product is designed to provide insights and analysis on maritime incidents, focusing on collision scenarios in daylight and good visibility conditions. Users are advised to review the detailed assessment provided in the manual to understand the factors contributing to the incident. Key points to consider:
- Ensure proper radar operation and target acquisition.
- Maintain vigilance and update vessel status as required.
- Activate audible alarms and monitor ECDIS unit settings.
Leak while bunkering caught in time (MARS 202436)
This section highlights a case study involving a leak during bunkering operations. To prevent similar incidents, users should follow these guidelines:
- Conduct thorough inspections of hoses before use.
- Maintain constant vigilance during bunkering operations.
- Ensure proper testing and maintenance of equipment.
Chemical burn due to inadequate PPE (MARS 202437)
To avoid chemical-related injuries during cleaning procedures, it is essential to adhere to the following safety measures:
- Ensure proper fitting and overlap of PPE.
- Regularly inspect and replace damaged or ill-fitting protective gear.
- Provide adequate training on handling hazardous substances.
MARS 202435
Collision in daylight and good visibility
As edited from MAIB (UK) preliminary assessment 3/24 https://tinyurl.com/MARS202435
In daylight and good visibility, cargo vessel A was making about 12 knots with a lone OOW on the bridge. Auto-pilot was being used for helm control and the OOW was occupied with administrative tasks. The radar was on but targets were not being acquired and alarms were not activated.
Meanwhile, about five nm away from vessel A, vessel B had recently stopped and
was drifting due to technical difficulties with the main engine. This vessel’s
lone OOW had not updated the vessel status to ‘not under command’ (NUC) on the
AIS, nor were the required NUC day signals raised. Vessel A maintained its
course and speed, with a steady bearing and decreasing range to vessel B.
Over the next 20 minutes, vessel A’s OOW continued to undertake other duties
on the bridge and was not monitoring nearby traffic. As vessel A approached
the drifting vessel B on a virtual collision course a crew member who had been
working on deck ran to the bridge and alerted the OOW to the developing
situation. Still making a speed of 12 knots, the OOW immediately used the
autopilot to initiate a turn to starboard before switching to hand steering to
increase the rudder angle. However, the turn was not sufficient to avoid
collision 10 seconds later. Vessel A’s port side struck vessel B’s starboard
quarter, resulting in hull damage to both vessels above the waterline.
The preliminary assessment found, among other things, that the ECDIS unit on
both vessels was set to silent mode, with all audible alarms deactivated while
underway. Also, although vessel B was visible on both of vessel A’s radars,
the target had not been acquired on the ARPA.
Lessons learned
- An OOW should actively navigate the vessel and not undertake any other tasks, ever!
- Activated alarms are an asset when at sea – use them.
- If your vessel’s navigational situation changes, set the appropriate instruments and signals to reflect this change in status.
MARS 202436
Leak while bunkering caught in time
A tanker had berthed for discharge operations and had also ordered bunkers. A bunker barge arrived at about 2:15 in the morning and was secured on the port side of the tanker. The bunker hose, supplied by the bunker barge, was connected to the tanker’s bunker manifold and surveyed to the extent possible by the tanker crew. Everything appeared correct and bunkering commenced with an initial rate of 40 tonnes/hr.
The bunkering station reported normal operations and no leaks so
the rate was gradually increased to 180 tonnes/hr. Soon after the rate
increase, a minor leak was observed in the hose and the bunkering was stopped.
A small quantity of oil had spread on deck and was cleaned. No oil was seen to
be released into the sea.
The bunker hose had apparently been tested under pressure four months earlier
but was now clearly less than adequate for the job.
Lessons learned
- Visual inspection of a bunker hose before use is necessary but cannot guarantee the integrity of the hose under full operating pressure.
- Vigilance at the bunkering station is a primary defence against pollution. When bunkering in darkness, ensure the hose is well lit and visible along its entire length.
MARS 202437
Chemical burn due to inadequate PPE
Cleaning procedures were in progress on a vessel’s empty holds. A solution of water and chemicals with a high alkaline value was being applied via a spray nozzle. Crew were protected with personal protective equipment (PPE) including chemical suits and rubber boots.
One crew member’s chemical suit was somewhat short and there was insufficient overlap with the boots. During the cleaning process, spray droplets on the chemical suit trickled down the length of the suit and entered the boots. The crew member continued to work unperturbed. Later, when he removed the boots, he saw his feet had been burned by the alkaline solution.
Providing learning through confidential reports – an international co- operative scheme for improving safety
Lessons learned
- It would appear the crew did not realise the extent of the risk of exposure to the washing solution. High alkaline or acidic levels always require maximum protection and awareness.
- The gap between the chemical suit and the boots was not noticed or was considered inconsequential. A STOP WORK action would have been appropriate if it had been noticed.
MARS 202438
It would appear the crew did not realise the extent of the risk of exposure to
the washing solution. High alkaline or acidic levels always require maximum
protection and awareness.
The gap between the chemical suit and the boots was not noticed or was
considered inconsequential. A STOP WORK action would have been appropriate if
it had been noticed.
False engine alarm causes collision
As edited from NTSB (U.S.A.) report MIR-23-16 https://tinyurl.com/MARS202438
Engine personnel on a partially loaded cargo vessel performed maintenance while at anchor to replace a failed cylinder head gasket. The vessel then took on a pilot and was inbound for the port to discharge the remaining cargo. Meanwhile, another vessel, also under pilotage, was outbound. The pilots had made arrangements over VHF radio to pass port to port at the Outer Bar Channel where the width of the navigable waterway was about 245m.
Shortly before the two vessels met, the main engine alarm detection panel on the inbound vessel recorded a high oil mist density reading, and the main engine shut down automatically. This also caused the loss of the bow thruster. The remaining electrical equipment and instruments, including the steering gear, continued to be powered. The vessel was now drifting and Not Under Command (NUC).
The pilot aboard the drifting NUC inbound vessel broadcast over VHF radio that
the vessel had lost propulsion and the vessel started veering to port. The
pilot ordered hard starboard rudder and instructed the captain to ‘sound the
danger signal’. The pilot confirmed the rudder’s response on the rudder angle
indicator, but, despite maintaining hard starboard rudder, the bow of the
drifting vessel continued veering to port, across the channel and toward the
path of the outbound vessel. Without propellor thrust the helm was virtually
useless.
On hearing the VHF radio broadcast, the pilot of the outbound vessel ordered
the vessel’s rudder hard to starboard and an increase of main engine speed by
10 rpm in an attempt to manoeuvre away from the approaching NUC vessel. Faced
with the NUC vessel cutting across
the channel, he ordered the rudder to midship, and then ordered a hard port
rudder. He believed this manoeuvre was now the only way to avoid contact with
the drifting vessel.
Two minutes after having lost main propulsion and with the NUC vessel still
moving at a speed of 7.4 knots and the outbound vessel
at 9.3 knots, the bow of the NUC vessel struck the port quarter of the
outbound, peeling back about 12 metres of that vessel’s hull plating forward
of the transom and wrapping it around the stern.
The official investigation found that the automatic shutdown of main engine on
the inbound vessel was likely due to a false alarm. The investigation posited
that the oil mist detector had sensed water vapour resulting from the engine
maintenance and incorrectly identified it as oil mist. This had falsely
triggered the alarm and ensured the automatic shutdown.
Lessons learned
- Cooling water can be introduced into engine lube oil systems during maintenance. Ambient air conditions, such as high humidity or extreme cold temperatures, can also increase the water content within engine lube oil sumps. An elevated quantity of water in lube oil systems can trigger false alarms in engine crankcase oil mist detectors (and lead to an engine shutdown).
- After an engine’s crankcase is opened and exposed to cold or humid conditions during maintenance and repair, it is good practice for engine crews to inspect and test the lubricating oil system for water intrusion and ensure lube oil purifying equipment is functioning properly to remove any water or other contamination in the lube oil.
MARS 202439
BRM failure contributes to shore contact
As edited from TAIC (New Zealand) report MO-2016-202 https://tinyurl.com/MARS202439
A passenger vessel was inbound for a port in daylight conditions. Visibility was moderate, but still in excess of one nm. Under the effect of the tidal stream, the vessel was travelling at 12 knots. A pilot was taken on board before entering the more restricted waters closer to the port area, and an exchange of information was accomplished. When the pilot asked about the turning characteristics of the vessel, the Master mentioned that the ship was highly maneuverable and would ‘turn on a dime’. He added that a three-degree helm order would create a rate of turn of 10-15 degrees per minute.
As the vessel approached the first turn to port, the pilot was concerned that
too much initial port helm would be detrimental
due to the tidal push from the northeast. Recognizing the good maneuverability
of the vessel, he ordered three degrees of port helm. By now the vessel was
making almost 18 knots due to the tidal stream partially astern.
Although a navigation officer was assigned duties at the ECDIS and
radar, at no point did he give data on the vessel’s progress such as actual
track versus planned track. Nonetheless, the pilot soon realized that the ship
was not turning to port as expected, so he ordered five degrees of port rudder
followed by 10 degrees in quick succession. The ship was now to the right of
the intended track and the cross-track distance from the intended track was
increasing rapidly to starboard.
The staff captain noticed the predictor on the ECDIS/Radar display had the
ship passing over the land ahead and to starboard. He suggested to the Master
that they increase the rate of turn. The Master reassured the staff captain
that the cross currents were strong and would bring the ship back to the
middle of the channel, reiterating what the pilot had explained during the
pilot/Master information exchange.
Soon, an off-track alarm visually flashed on the ECDIS, although audible
alarms had been muted before entering the restricted waterway. The ship had
departed the predefined safety corridor either side of the planned track, but
this information was not brought to the attention of the Master or pilot. Yet,
by now they both realized that the ship was proceeding dangerously close to
the rocks on the starboard side. Twenty degrees of port rudder was ordered,
immediately followed by maximum port rudder. The ship responded with a rapid
turn to port. When the ship was approaching the closest point to the rocks on
the starboard side, the Master ordered maximum helm to starboard in an attempt
to arrest the rapid port turn and prevent the stern from striking the rocks.
The ship’s bilge keel and the starboard propeller nonetheless made contact as
they passed the rocks. The ship was then navigated back to the centre of the
channel and continued on its passage to port without further incident.
Lessons learned
- The concept of allowing a ship to depart from an intended track in the belief that other influences, such as tide in this case, would return the ship to that track carries a high risk when maneuvering large ships in narrow waterways where margins for error are small. There is less risk involved when a ship is kept strictly to the intended track by increasing or decreasing its rate of turn in response to the influences of factors such as tide and wind.
- Also, the above maneuvering method leaves other members of the bridge team tasked with monitoring the progress of the ship against the planned track in limbo. How can an officer or Master ‘challenge’ the person with the con if the situation is intentionally obscure or undefined?
- Good BRM practices help to ensure that the best decisions are made and any errors or malfunctions of equipment are identified and corrected before an incident can develop. In order to achieve this objective and navigate a ship safely, a shared understanding of the passage plan by the entire bridge team is critical.
MARS 202440
Are your watertight doors watertight?
As edited from IMCA Safety Flash 08-24 https://tinyurl.com/MARS202440
During a safety walkaround on a vessel, it was observed that several type C watertight doors (doors that must remain closed at all times and opened only when personnel pass through them) were routinely kept open while underway. It was expressly indicated in the vessel’s procedures that these doors must remain closed while at sea.
A review of similar cases on two other fleet vessels found that watertight doors were left open after the regular engine room walk around, as this was a regular activity and there was ‘no point to open and close [them] each time.’ It was also found that some crew were not aware of the relevant SOLAS and SMS requirements or the importance of keeping type C watertight doors closed at sea in case of emergency.
Lessons learned
- Watertight doors are critical elements in preventing the ingress of water from one compartment to another during flooding or accidents. The seaworthiness of the vessel depends on their proper use.
- As with many safety-critical elements on a vessel, acceptance of procedures such as keeping type C watertight doors closed by crew is dependent on the safety leadership of senior officers and the Master.
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Frequently Asked Questions
Q: How can I ensure safe bunkering operations?
A: Conduct visual inspections of hoses, maintain proper lighting, and monitor operations closely to detect any leaks or issues promptly.
Q: What should I do in case of a chemical exposure incident?
A: Seek immediate medical attention, remove contaminated clothing, and rinse the affected area with water. Follow established protocols for chemical exposure emergencies.
References
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- Home | ABC Maritime AG
- Aims Institute of Maritime Studies
- A R Brink & Associates Marine Surveyors - Marine Surveyors & Consultants in Durban South Africa
- Chevron Corporation - Human Energy — Chevron
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- KASI (Malaysia) - Your Partner in Progress
- Home - Louis Dreyfus Armateurs
- Working With the Royal Navy and Maritime Community | MSSC
- MARS
- Norwegian Hull Club | norclub.com
- Ferry to the Orkney and Shetland islands | NorthLink Ferries
- Port of London Authority | Port of London Authority
- Poseidon
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- INICIO
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- Home
- Mitsui O.S.K. Lines, Ltd.
- Poseidon Maritime
- SQLearn Maritime Training • ONLINE CBT platform
- Homepage - Stargate Crewing
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